KIS-List Digest Archive

Mon 03/27/17


Total Messages Posted: 13



Today's Message Index:
----------------------
 
     1. 06:20 AM - Re: Can anybody confirm this? (mark_trickel)
     2. 07:52 AM - Re: Re: Can anybody confirm this? (Keith.Miller@esa.int)
     3. 10:22 AM - Re: Re: Can anybody confirm this? (Owen Baker)
     4. 10:50 AM - Re: Re: Can anybody confirm this? (pastormac@comcast.net)
     5. 12:00 PM - Re: Can anybody confirm this? (Owen Baker)
     6. 01:27 PM - Fw: Re: Can anybody confirm this? (Owen Baker)
     7. 01:47 PM - Re: Re: Can anybody confirm this? (Galin Hernandez)
     8. 01:47 PM - Re: Re: Can anybody confirm this? (Galin Hernandez)
     9. 02:05 PM - Re: Fw: Re: Can anybody confirm this? (Galin Hernandez)
    10. 02:07 PM - Re: Fw: Re: Can anybody confirm this? (Galin Hernandez)
    11. 02:08 PM - Re: Can anybody confirm this? (M Ketteing)
    12. 04:42 PM - Re: Re: Can anybody confirm this? (pastormac@comcast.net)
    13. 05:13 PM - Re: Re: Can anybody confirm this? (Galin Hernandez)
 
 
 


Message 1


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    Time: 06:20:44 AM PST US
    Subject: Re: Can anybody confirm this?
    From: "mark_trickel" <marktrickel@gmail.com>
    OC, thank you for the details of this situation. When any occurrence happens within our small community I feel it is very important that all details are covered so we can learn from it. The unfortunate part is that only a very small percentage of our community frequent this forum. I was aware you were having Lyle make you a new nose gear with changes. I was aware you were looking for torque specs, but I missed the mishap. My questions are: On nose gear #1 That was a little disheartening to learn the stud was too short to allow for a proper stack, and that the hole was off center and too close to the end of the stud. Now that makes me fearful about the rest of the fleet that might have this nose gear version. I am curious to know if you might have considered milling the surface of the shoe to allow of a proper stack? That may have eliminated one of your two issues and a proper stack with Belleville washers in place could have remedied your second issue to only having to modified the castle nut in one cotter pin slot. What was in your original stack? On nose gear #2 What was in the stack? Did you have steel washers on both sides (above and below) of the Belleville washers? Did you have the Belleville washers in direct contact with the aluminum shoe? Weight and balance Where do you estimate your CG was at the time of this episode? We all know the forward and aft limits of the TR-1 but simply having the CG at the forward limit is not good enough (IMO). The CG needs to be closer to the center and in the best-case scenario closer to the aft limit as that is where it is most efficient. So I understand you had a nose gear collapse similar to Galin. Your spinner hit the runway. The engine was most likely at idol say 800 to 900 rpm at the time of impact. How many times did each blade strike the runway? And this prop was repairable? Nose gear #3 third time is always a charm! MT Read this topic online here: http://forums.matronics.com/viewtopic.php?p=467672#467672


    Message 2


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    Time: 07:52:29 AM PST US
    Subject: Re: Can anybody confirm this?
    From: Keith.Miller@esa.int
    I think it was a bit a bad luck with OC 's shortened stud . Mine was made a few months later by Lyle and he had noted the problem and fixed it, so i guess it depends upon when it was made in the production series (See attached file: IMG_9929.JPG) From: "mark_trickel" <marktrickel@gmail.com> Subject: KIS-List: Re: Can anybody confirm this? Sent by: owner-kis-list-server@matronics.com OC, thank you for the details of this situation. When any occurrence happens within our small community I feel it is very important that all details are covered so we can learn from it. The unfortunate part is that only a very small percentage of our community frequent this forum. I was aware you were having Lyle make you a new nose gear with changes. I was aware you were looking for torque specs, but I missed the mishap. My questions are: On nose gear #1 ??? That was a little disheartening to learn the stud was too short to allow for a proper stack, and that the hole was off center and too close to the end of the stud. Now that makes me fearful about the rest of the fleet that might have this nose gear version. I am curious to know if you might have considered milling the surface of the shoe to allow of a proper stack? That may have eliminated one of your two issues and a proper stack with Belleville washers in place could have remedied your second issue to only having to modified the castle nut in one cotter pin slot. What was in your original stack? On nose gear #2 ??? What was in the stack? Did you have steel washers on both sides (above and below) of the Belleville washers? Did you have the Belleville washers in direct contact with the aluminum shoe? Weight and balance ??? Where do you estimate your CG was at the time of this episode? We all know the forward and aft limits of the TR-1 but simply having the CG at the forward limit is not good enough (IMO). The CG needs to be closer to the center and in the best-case scenario closer to the aft limit as that is where it is most efficient. So I understand you had a nose gear collapse similar to Galin. Your spinner hit the runway. The engine was most likely at idol say 800 to 900 rpm at the time of impact. How many times did each blade strike the runway? And this prop was repairable? Nose gear #3 ??? third time is always a charm! MT Read this topic online here: http://forums.matronics.com/viewtopic.php?p=467672#467672 This message and any attachments are intended for the use of the addressee or addressees only. The unauthorised disclosure, use, dissemination or copying (either in whole or in part) of its content is not permitted. If you received this message in error, please notify the sender and delete it from your system. Emails can be altered and their integrity cannot be guaranteed by the sender. Please consider the environment before printing this email. This message and any attachments are intended for the use of the addressee or addressees only. The unauthorised disclosure, use, dissemination or copying (either in whole or in part) of its content is not permitted. If you received this message in error, please notify the sender and delete it from your system. Emails can be altered and their integrity cannot be guaranteed by the sender. Please consider the environment before printing this email.


    Message 3


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    Time: 10:22:11 AM PST US
    From: "Owen Baker " <bakerocb@cox.net>
    Subject: Re: Can anybody confirm this?
    3/27/2017 Hello Keith, Thanks for your input. You wrote: 1) ".... he had noted the problem and fixed it..." I don't think so. Your picture appears to also show a thin AN320-12 shear type castle nut in place with a fairly thin washer stack up (Bellevilles?). This would be consistent with the same length of the 3/4 inch diameter portion of the vertical stub as my #1 Lyle gear. I have seen no evidence that Lyle changed the length of the 3/4 inch diameter portion of the vertical stub until (at my request) he made it a bit longer for my #2 and #3 weldments. See the attached picture of the vertical stub on my #1 Lyle nose gear. I initially thought that the 3/4 inch diameter portion of the vertical stub was a machined out and threaded continuation of the vertical stub steel immediately above it (all one solid piece). I later learned that I was wrong and that the 3/4 inch diameter portion was, in fact, a separately obtained bolt whose head (maybe machined round first) was inserted into a hole in the steel above it and welded into place. Only after removing my #1 Lyle gear from the plane and examining the end of the vertical stub with a bright light and a magnifying glass was I able to see the evidence of a weld bead. I speculate that Lyle obtained these bolts from McMaster-Carr and that the quality control of the original manufacturer of these bolts was not pristine. The cotter pin holes were not exactly through the center of the bolt (I have noticed a bit of this on the bolts in my #2 and #3 Lyle gears as well) and the cotter pin hole in the end of the bolt in my #1 Lyle gear was too close to the end of the bolt for my comfort. Any questions? OC ============================================ From: Keith.Miller@esa.int Sent: Monday, March 27, 2017 10:45 AM Subject: Re: KIS-List: Re: Can anybody confirm this? I think it was a bit a bad luck with OC 's shortened stud . Mine was made a few months later by Lyle and he had noted the problem and fixed it, so i guess it depends upon when it was made in the production series


    Message 4


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    Time: 10:50:53 AM PST US
    From: pastormac@comcast.net
    Subject: Re: Can anybody confirm this?
    Hi Guys, Speaking of the nose gear. I'm getting quite a bit of shimmy on take off and landing. Is there an adjustment I can make? Thanks!! Steve Sent from my iPhone > On Mar 27, 2017, at 1:21 PM, Owen Baker <bakerocb@cox.net> wrote: > > 3/27/2017 > > Hello Keith, Thanks for your input. You wrote: > > 1) ".... he had noted the problem and fixed it..." > > I don't think so. Your picture appears to also show a thin AN320-12 shear type castle nut in place with a fairly thin washer stack up (Bellevilles?). This would be consistent with the same length of the 3/4 inch diameter portion of the vertical stub as my #1 Lyle gear. I have seen no evidence that Lyle changed the length of the 3/4 inch diameter portion of the vertical stub until (at my request) he made it a bit longer for my #2 and #3 weldments. > > See the attached picture of the vertical stub on my #1 Lyle nose gear. I initially thought that the 3/4 inch diameter portion of the vertical stub was a machined out and threaded continuation of the vertical stub steel immediately above it (all one solid piece). I later learned that I was wrong and that the 3/4 inch diameter portion was, in fact, a separately obtained bolt whose head (maybe machined round first) was inserted into a hole in the steel above it and welded into place. Only after removing my #1 Lyle gear from the plane and examining the end of the vertical stub with a bright light and a magnifying glass was I able to see the evidence of a weld bead. > > I speculate that Lyle obtained these bolts from McMaster-Carr and that the quality control of the original manufacturer of these bolts was not pristine. The cotter pin holes were not exactly through the center of the bolt (I have noticed a bit of this on the bolts in my #2 and #3 Lyle gears as well) and the cotter pin hole in the end of the bolt in my #1 Lyle gear was too close to the end of the bolt for my comfort. > > Any questions? > > OC > > ============================================ > > From: Keith.Miller@esa.int > Sent: Monday, March 27, 2017 10:45 AM > To: kis-list@matronics.com > Subject: Re: KIS-List: Re: Can anybody confirm this? > > I think it was a bit a bad luck with OC 's shortened stud . Mine was made a > few months later by Lyle and he had noted the problem and fixed it, so i > guess it depends upon when it was made in the production series > > > <4-9-16 CAMERA 003.JPG>


    Message 5


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    Time: 12:00:55 PM PST US
    From: "Owen Baker " <bakerocb@cox.net>
    Subject: Re: Can anybody confirm this?
    3/27/2017 Hello Mark, You wrote: 1) "I am curious to know if you might have considered milling the surface of the shoe to allow of a proper stack?" This is not a feasible solution. The bottom surface of the shoe must project down below the shoulder above the 3/4 inch diameter portion of the vertical stub so that any washers contact the bottom of the shoe and not the shoulder of the stub. This washer contact with the bottom of the shoe is what applies the friction force on the shoe that keeps it from shimmying. In one of the newsletters there is an article, along with a sketch, that emphasizes this point. 2) "... a proper stack with Belleville washers in place could have remedied your second issue to only having to modified the castle nut in one cotter pin slot." I operated with only one pair of widened notches in the castle nut for some period of time. This became a nuisance when I wanted to make a small friction adjustment without disturbing and reshuffling the entire washer stack. What you are suggesting here is that the friction level be adjusted by inserting or removing washers to obtain the desired results rather than just turning the nut. This is a rather crude manner of adjusting the friction and it could take many tries (and many different washer thicknesses) to achieve the desired results. As a side note: Realize also that the nut must be prevented from rotating by sticking an ice pick or something similar through the cotter key passage every time the shoe is rotated for testing of the friction level. It always bothered me a bit that the nut rotated back and forth a little bit with the change in direction of the movement of the shoe even with the cotter pin in place. I eventually solved that problem, if it was a problem, by replacing the cotter pin with a #6 hex socket head cap screw, two washers, and an elastic stop nut. 3) "What was in your original stack?" One or more 1/8 inch thick nylon washers and flat metal washers as needed to fit in the limited height available and obtained the desired friction level. 4) "On nose gear #2 What was in the stack?" Either two or four Belleville washers -- I can not exactly recall. 5) "Did you have steel washers on both sides (above and below) of the Belleville washers?" I did not. Even with the provided increased length of the 3/4 inch diameter portion of the vertical stub there was insufficient room to accommodate flat washers in addition to the Belleville washers and the full size AN310-12 castle nut. (I had asked Lyle to make the 3/4 inch portion of the vertical stub longer than he provided, but he declined to do so.) 6) "Did you have the Belleville washers in direct contact with the aluminum shoe?" Yes, but it was not my desire to do it that way. See 5 above. 7) "Where do you estimate your CG was at the time of this episode?" Some where between 61.50 and 65.60 inches aft of the datum point. 8) "How many times did each blade strike the runway?" Here is how I responded to a local pilot who asked a similarly motivated question about engine stoppage: "The engine did not experience sudden stoppage in the current factory documented concept in my opinion. First point: This is a wooden prop and all the current literature assumes a metal prop which can deliver a much more abrupt shock to an engine crankshaft. Second point: Each of the propeller blades had a small and equal amount of material scraped off of its tip with no significant impact rotational damage appearing any further towards the propeller hub. I considered pulling the engine and sending it to one of the three organizations that the factory rep recommended when I talked to him about my situation. I also reviewed the Continental documentation on what they considered an acceptable tear down inspection. It was practically back to the ore that the metal had been forged from -- no bit was to be left connected to any other bit. I also thought back to my training at the Continental factory before I bought my engine and remembered the tooling, extreme precision, and care that was needed in assembling an engine. I just did not believe that: a) That degree of disassembly was needed. b) No field activity in their right mind would go to the disassembly level called for in the Continental documentation. c) Regardless of the level of disassembly at the field activity I doubted their ability to put the engine back together as well as it was currently put together by the factory. I had more confidence in the engine as it existed than after a tear down and reassembly by some non factory field activity." 9) "And this prop was repairable?" The tips were repaired by the Prince factory in a few weeks and the engine, prop, plane, and pilot have flown 15 hours since the event. OC PS: I can appreciate that people are reading all sorts of things into this event and asking all sorts of questions that I am willing to answer. But I ask all to remember that this event was a direct result of the mechanic (me) installing Lyle gear #2 with no numerical friction level information at hand and using the criteria of TFAR (That Feels About Right) to set the friction level. It was right for a few landings and then it wasn't. ============================== From: mark_trickel Sent: Monday, March 27, 2017 9:19 AM Subject: KIS-List: Re: Can anybody confirm this? OC, thank you for the details of this situation. When any occurrence happens within our small community I feel it is very important that all details are covered so we can learn from it. The unfortunate part is that only a very small percentage of our community frequent this forum. I was aware you were having Lyle make you a new nose gear with changes. I was aware you were looking for torque specs, but I missed the mishap. My questions are: On nose gear #1 That was a little disheartening to learn the stud was too short to allow for a proper stack, and that the hole was off center and too close to the end of the stud. Now that makes me fearful about the rest of the fleet that might have this nose gear version. I am curious to know if you might have considered milling the surface of the shoe to allow of a proper stack? That may have eliminated one of your two issues and a proper stack with Belleville washers in place could have remedied your second issue to only having to modified the castle nut in one cotter pin slot. What was in your original stack? On nose gear #2 What was in the stack? Did you have steel washers on both sides (above and below) of the Belleville washers? Did you have the Belleville washers in direct contact with the aluminum shoe? Weight and balance Where do you estimate your CG was at the time of this episode? We all know the forward and aft limits of the TR-1 but simply having the CG at the forward limit is not good enough (IMO). The CG needs to be closer to the center and in the best-case scenario closer to the aft limit as that is where it is most efficient. So I understand you had a nose gear collapse similar to Galin. Your spinner hit the runway. The engine was most likely at idol say 800 to 900 rpm at the time of impact. How many times did each blade strike the runway? And this prop was repairable? Nose gear #3 third time is always a charm! MT


    Message 6


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    Time: 01:27:20 PM PST US
    From: "Owen Baker " <bakerocb@cox.net>
    Subject: Re: Can anybody confirm this?
    3/27/2017 Hello Steve, You wrote: "Is there an adjustment I can make?" This is very dangerous. DO NOT FLY THIS PLANE until the friction nut on the bottom of the nose gear has been properly adjusted. See the photo from Keith Miller (thanks Keith) that is attached to this email. This shimmy can become violent enough to damage the nose gear linkages, collapse the nose gear, and cause the nose of the airplane to fall down and contact the runway surface. I recommend: 1) Elevate the nose of the plane so that the nose tire is off the ground. (Contact me if needed for tips on how to do this.) 2) Attach a fish scale to the shoe holding the nose wheel in the vicinity of the wheel axle. See how many pounds of pull that it takes to move the shoe from side to side. This is to establish what the friction level is now. If it is several pounds less than 27 pounds (which it probably is because of the shimmy) you must adjust the friction level. 3) Use a black sharpie pen to number the nut notch above the cotter pin head as notch 1. Make a vertical mark on the shoe above notch 1 with the sharpie. 4) Remove the cotter pin holding the large AN320-12 castle nut from turning. Go around the nut with the sharpie numbering each notch in sequence. This is so that you can keep track of the notch that is under the vertical mark. 5) Using a 1 1/8 inch box wrench tighten the nut one notch. Use an ice pick or similar item to ensure that the new nut notch and the cotter pin hole through the vertical stub are aligned. Leave the ice pick in place. 6) Use the fish scale again to move the shoe back and forth to ensure that you have adjusted the friction to the vicinity of 27 pounds. 7) Remove the ice pick and repeat 5 and 6 above if needed. When you have the desired friction level set, install a new cotter pin and lower the nose tire to the ground. 8) Go fly the plane. Any questions? OC =============================== From: pastormac@comcast.net Sent: Monday, March 27, 2017 1:50 PM Subject: Re: KIS-List: Re: Can anybody confirm this? Hi Guys, Speaking of the nose gear. I'm getting quite a bit of shimmy on take off and landing. Is there an adjustment I can make? Thanks!! Steve


    Message 7


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    Time: 01:47:36 PM PST US
    From: Galin Hernandez <galinhdz@gmail.com>
    Subject: Re: Can anybody confirm this?
    FWIW Rich told me to adjust the nose gear friction to between 20 and 35lbs of break force with 27lb being optimal. He did say that 20lbs was an absolute minimum, that 20lbs might not work in some cases and not to worry about being super accurate. I still have the cheap Walmart fish weight scale he got for me in El Salvador just like this one: https://www.walmart.com/ip/Berkley-Scale-with-Tape/16637411 I try to adjust mine for 27lbs but take anything over 25lbs. This has worked well for me in the last 10yrs of flying my TR-4. YMMV On Mon, Mar 27, 2017 at 1:50 PM, <pastormac@comcast.net> wrote: > > Hi Guys, > Speaking of the nose gear. I'm getting quite a bit of shimmy on take off > and landing. Is there an adjustment I can make? > Thanks!! > Steve > > Sent from my iPhone > > > On Mar 27, 2017, at 1:21 PM, Owen Baker <bakerocb@cox.net> wrote: > > > > 3/27/2017 > > > > Hello Keith, Thanks for your input. You wrote: > > > > 1) ".... he had noted the problem and fixed it..." > > > > I don't think so. Your picture appears to also show a thin AN320-12 > shear type castle nut in place with a fairly thin washer stack up > (Bellevilles?). This would be consistent with the same length of the 3/4 > inch diameter portion of the vertical stub as my #1 Lyle gear. I have seen > no evidence that Lyle changed the length of the 3/4 inch diameter portion > of the vertical stub until (at my request) he made it a bit longer for my > #2 and #3 weldments. > > > > See the attached picture of the vertical stub on my #1 Lyle nose gear. I > initially thought that the 3/4 inch diameter portion of the vertical stub > was a machined out and threaded continuation of the vertical stub steel > immediately above it (all one solid piece). I later learned that I was > wrong and that the 3/4 inch diameter portion was, in fact, a separately > obtained bolt whose head (maybe machined round first) was inserted into a > hole in the steel above it and welded into place. Only after removing my #1 > Lyle gear from the plane and examining the end of the vertical stub with a > bright light and a magnifying glass was I able to see the evidence of a > weld bead. > > > > I speculate that Lyle obtained these bolts from McMaster-Carr and that > the quality control of the original manufacturer of these bolts was not > pristine. The cotter pin holes were not exactly through the center of the > bolt (I have noticed a bit of this on the bolts in my #2 and #3 Lyle gears > as well) and the cotter pin hole in the end of the bolt in my #1 Lyle gear > was too close to the end of the bolt for my comfort. > > > > Any questions? > > > > OC > > > > ============================================ > > > > From: Keith.Miller@esa.int > > Sent: Monday, March 27, 2017 10:45 AM > > To: kis-list@matronics.com > > Subject: Re: KIS-List: Re: Can anybody confirm this? > > > > I think it was a bit a bad luck with OC 's shortened stud . Mine was > made a > > few months later by Lyle and he had noted the problem and fixed it, so i > > guess it depends upon when it was made in the production series > > > > > > <4-9-16 CAMERA 003.JPG> > >


    Message 8


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    Time: 01:47:55 PM PST US
    From: Galin Hernandez <galinhdz@gmail.com>
    Subject: Re: Can anybody confirm this?
    Wrong Walmart link. THIS is the one I have https://www.walmart.com/ip/Eagle-Claw-Scale-with-Tape-Measure-50-lb/45087468 On Mon, Mar 27, 2017 at 4:45 PM, Galin Hernandez <galinhdz@gmail.com> wrote: > FWIW Rich told me to adjust the nose gear friction to between 20 and 35lbs > of break force with 27lb being optimal. He did say that 20lbs was an > absolute minimum, that 20lbs might not work in some cases and not to worry > about being super accurate. I still have the cheap Walmart fish weight > scale he got for me in El Salvador just like this one: > > https://www.walmart.com/ip/Berkley-Scale-with-Tape/16637411 > > I try to adjust mine for 27lbs but take anything over 25lbs. This has > worked well for me in the last 10yrs of flying my TR-4. YMMV > > On Mon, Mar 27, 2017 at 1:50 PM, <pastormac@comcast.net> wrote: > >> >> Hi Guys, >> Speaking of the nose gear. I'm getting quite a bit of shimmy on take off >> and landing. Is there an adjustment I can make? >> Thanks!! >> Steve >> >> Sent from my iPhone >> >> > On Mar 27, 2017, at 1:21 PM, Owen Baker <bakerocb@cox.net> wrote: >> > >> > 3/27/2017 >> > >> > Hello Keith, Thanks for your input. You wrote: >> > >> > 1) ".... he had noted the problem and fixed it..." >> > >> > I don't think so. Your picture appears to also show a thin AN320-12 >> shear type castle nut in place with a fairly thin washer stack up >> (Bellevilles?). This would be consistent with the same length of the 3/4 >> inch diameter portion of the vertical stub as my #1 Lyle gear. I have seen >> no evidence that Lyle changed the length of the 3/4 inch diameter portion >> of the vertical stub until (at my request) he made it a bit longer for my >> #2 and #3 weldments. >> > >> > See the attached picture of the vertical stub on my #1 Lyle nose gear. >> I initially thought that the 3/4 inch diameter portion of the vertical stub >> was a machined out and threaded continuation of the vertical stub steel >> immediately above it (all one solid piece). I later learned that I was >> wrong and that the 3/4 inch diameter portion was, in fact, a separately >> obtained bolt whose head (maybe machined round first) was inserted into a >> hole in the steel above it and welded into place. Only after removing my #1 >> Lyle gear from the plane and examining the end of the vertical stub with a >> bright light and a magnifying glass was I able to see the evidence of a >> weld bead. >> > >> > I speculate that Lyle obtained these bolts from McMaster-Carr and that >> the quality control of the original manufacturer of these bolts was not >> pristine. The cotter pin holes were not exactly through the center of the >> bolt (I have noticed a bit of this on the bolts in my #2 and #3 Lyle gears >> as well) and the cotter pin hole in the end of the bolt in my #1 Lyle gear >> was too close to the end of the bolt for my comfort. >> > >> > Any questions? >> > >> > OC >> > >> > ============================================ >> > >> > From: Keith.Miller@esa.int >> > Sent: Monday, March 27, 2017 10:45 AM >> > To: kis-list@matronics.com >> > Subject: Re: KIS-List: Re: Can anybody confirm this? >> > >> > I think it was a bit a bad luck with OC 's shortened stud . Mine was >> made a >> > few months later by Lyle and he had noted the problem and fixed it, so >> i >> > guess it depends upon when it was made in the production series >> > >> > >> > <4-9-16 CAMERA 003.JPG> >> >> >> >> >> >> >


    Message 9


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    Time: 02:05:42 PM PST US
    From: Galin Hernandez <galinhdz@gmail.com>
    Subject: Re: Can anybody confirm this?
    OC wrote: "This shimmy can become violent enough to damage the nose gear linkages, collapse the nose gear, and cause the nose of the airplane to fall down and contact the runway surface." Heed these WORDS OF WISDOM!!! If you have experienced noticeable shimmy, I recommend you replace the bolts/pin that hold the nose gear "H" bracket. With the nose elevated so no weight is on the nose gear, remove the bolts/pin and check them for any signs of failure. Especially the rear ones. Without magnafluxing or some other NDI, you probably won't be able to tell if they are failing. That is why I feel it isn't even worth inspecting them, just replace the bolts with new ones. Cheap insurance. On Mon, Mar 27, 2017 at 4:26 PM, Owen Baker <bakerocb@cox.net> wrote: > 3/27/2017 > > Hello Steve, You wrote: "Is there an adjustment I can make?" > > This is very dangerous. DO NOT FLY THIS PLANE until the friction nut on > the bottom of the nose gear has been properly adjusted. > See the photo from Keith Miller (thanks Keith) that is attached to this > email. > > This shimmy can become violent enough to damage the nose gear linkages, > collapse the nose gear, and cause the nose of the airplane to fall down and > contact the runway surface. > > I recommend: > > 1) Elevate the nose of the plane so that the nose tire is off the ground. > (Contact me if needed for tips on how to do this.) > > 2) Attach a fish scale to the shoe holding the nose wheel in the vicinity > of the wheel axle. See how many pounds of pull that it takes to move the > shoe from side to side. This is to establish what the friction level is > now. If it is several pounds less than 27 pounds (which it probably is > because of the shimmy) you must adjust the friction level. > > 3) Use a black sharpie pen to number the nut notch above the cotter pin > head as notch 1. Make a vertical mark on the shoe above notch 1 with the > sharpie. > > 4) Remove the cotter pin holding the large AN320-12 castle nut from > turning. Go around the nut with the sharpie numbering each notch in > sequence. This is so that you can keep track of the notch that is under the > vertical mark. > > 5) Using a 1 1/8 inch box wrench tighten the nut one notch. Use an ice > pick or similar item to ensure that the new nut notch and the cotter pin > hole through the vertical stub are aligned. Leave the ice pick in place. > > 6) Use the fish scale again to move the shoe back and forth to ensure that > you have adjusted the friction to the vicinity of 27 pounds. > > 7) Remove the ice pick and repeat 5 and 6 above if needed. When you have > the desired friction level set, install a new cotter pin and lower the nose > tire to the ground. > > 8) Go fly the plane. > > Any questions? > > OC > > =============================== > > From: pastormac@comcast.net > Sent: Monday, March 27, 2017 1:50 PM > To: kis-list@matronics.com > Subject: Re: KIS-List: Re: Can anybody confirm this? > > > Hi Guys, > Speaking of the nose gear. I'm getting quite a bit of shimmy on take off > and landing. Is there an adjustment I can make? > Thanks!! > Steve


    Message 10


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    Time: 02:07:57 PM PST US
    From: Galin Hernandez <galinhdz@gmail.com>
    Subject: Re: Can anybody confirm this?
    Oh, and inspect the "H" bracket for any crack or sign of potential failure. On Mon, Mar 27, 2017 at 5:04 PM, Galin Hernandez <galinhdz@gmail.com> wrote: > OC wrote: "This shimmy can become violent enough to damage the nose gear > linkages, collapse the nose gear, and cause the nose of the airplane to > fall down and contact the runway surface." Heed these WORDS OF WISDOM!!! > If you have experienced noticeable shimmy, I recommend you replace the > bolts/pin that hold the nose gear "H" bracket. > > With the nose elevated so no weight is on the nose gear, remove the > bolts/pin and check them for any signs of failure. Especially the rear > ones. Without magnafluxing or some other NDI, you probably won't be able to > tell if they are failing. That is why I feel it isn't even worth > inspecting them, just replace the bolts with new ones. > > Cheap insurance. > > On Mon, Mar 27, 2017 at 4:26 PM, Owen Baker <bakerocb@cox.net> wrote: > >> 3/27/2017 >> >> Hello Steve, You wrote: "Is there an adjustment I can make?" >> >> This is very dangerous. DO NOT FLY THIS PLANE until the friction nut on >> the bottom of the nose gear has been properly adjusted. >> See the photo from Keith Miller (thanks Keith) that is attached to this >> email. >> >> This shimmy can become violent enough to damage the nose gear linkages, >> collapse the nose gear, and cause the nose of the airplane to fall down and >> contact the runway surface. >> >> I recommend: >> >> 1) Elevate the nose of the plane so that the nose tire is off the ground. >> (Contact me if needed for tips on how to do this.) >> >> 2) Attach a fish scale to the shoe holding the nose wheel in the vicinity >> of the wheel axle. See how many pounds of pull that it takes to move the >> shoe from side to side. This is to establish what the friction level is >> now. If it is several pounds less than 27 pounds (which it probably is >> because of the shimmy) you must adjust the friction level. >> >> 3) Use a black sharpie pen to number the nut notch above the cotter pin >> head as notch 1. Make a vertical mark on the shoe above notch 1 with the >> sharpie. >> >> 4) Remove the cotter pin holding the large AN320-12 castle nut from >> turning. Go around the nut with the sharpie numbering each notch in >> sequence. This is so that you can keep track of the notch that is under the >> vertical mark. >> >> 5) Using a 1 1/8 inch box wrench tighten the nut one notch. Use an ice >> pick or similar item to ensure that the new nut notch and the cotter pin >> hole through the vertical stub are aligned. Leave the ice pick in place. >> >> 6) Use the fish scale again to move the shoe back and forth to ensure >> that you have adjusted the friction to the vicinity of 27 pounds. >> >> 7) Remove the ice pick and repeat 5 and 6 above if needed. When you have >> the desired friction level set, install a new cotter pin and lower the nose >> tire to the ground. >> >> 8) Go fly the plane. >> >> Any questions? >> >> OC >> >> =============================== >> >> From: pastormac@comcast.net >> Sent: Monday, March 27, 2017 1:50 PM >> To: kis-list@matronics.com >> Subject: Re: KIS-List: Re: Can anybody confirm this? >> >> >> Hi Guys, >> Speaking of the nose gear. I'm getting quite a bit of shimmy on take off >> and landing. Is there an adjustment I can make? >> Thanks!! >> Steve > >


    Message 11


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    Time: 02:08:15 PM PST US
    From: M Ketteing <aeromomentum@yahoo.com>
    Subject: Re: Can anybody confirm this?
    Hi OC, In general you should have from 10% (max aft CG) to 25% (max forward CG) on the nose gear. Assuming your empty weight is a portly 903 lbs and you are at max forward CG, you should have no more than 225 lbs on your nose gear. My guess is even at full empty your CG is still not at the front limit. So you (like most every TR-1) still have too much weight on the nose gear. You really should move the main gear more forward. Based on 10% on the nose gear at max gross and max aft CG the main should be about 70.5 inches. I would go with about 71 inches. You really will like landing and taking off much more with this main gear location. Plus the loads and stress on the nose gear will be much less. Also keep in mind that when I checked the nose gear in 1999 (version 2.1, streamlined tube with added side plates) most everything did not meet FAR part 23 requirements. This includes the arms, pins and bolts along with the actual tube. I don't think most of these parts were upgraded with version 3.X. Mark K. -------------------------------------------- On Sun, 3/26/17, Owen Baker <bakerocb@cox.net> wrote: Subject: Re: KIS-List: Can anybody confirm this? To: kis-list@matronics.com, "TRICKEL MARK" <marktrickel@gmail.com>, "KETTERING MARK" <aeromomentum@yahoo.com> Date: Sunday, March 26, 2017, 6:29 PM "Owen Baker " <bakerocb@cox.net> 3/26/2017 Hello Mark K, Thanks for your input. You wrote: 1) "Have you moved you main gear forward?" Yes, I wedged it forward with flox. The main landing gear axles are 72.25 inches aft of the 0.00 datum point. That datum point is, in turn, 32.00 inches forward of the engine cowling joggle on the fuselage. 2) "How much weight do you have on your nose gear?" Right now, in operational configuration and without reweighing, I don't know. The original empty aircraft weighing showed 242 pounds on the nose gear. Since then there have been a few misc items (quart of oil, jar for fuel testing, rags, etc.) that are normally kept in the right baggage well. Also there are some other misc items (hand held radio, small tool bag, water bottle, roll of tape, etc.) that have taken up permanent lodging on the hat shelf aft of the seats. Not too long ago I double bagged sand into two kitchen sliding lock plastic gallon bags (they totaled 23 pounds) and placed them over the battery box in the far right rear corner of the right baggage well (I mostly fly solo in the left seat) because I was unhappy that the nose gear was descending to meet the runway too quickly after the main gear touched down. I am not sure if that has helped, or if so how much. 3) "The geometry (pivot axis angle) could maybe use some tweaking to reduce shimmy." Can you please elaborate on the contribution of the pivot angle axis on shimmy and how one would go about tweaking that angle in a KIS TR-1? Thanks. Also a reminder that my shimmy problem with strut #2 was my fault for not tightening the friction nut enough and I have had no shimmy problems since installing strut #3 and using 27 pounds as a base figure for setting the friction nut. Also in my listing of the design / manufacturing defects in the #1 strut in paragraph 1 below I forget to mention that the off center cotter pin hole was also so close to the end of the vertical stub that I was concerned about the possibility of break out. OC PS: I have your last name spelled Kettering in some old places in my computer. Has there been a change? ======================================= From: M Ketteing Sent: Sunday, March 26, 2017 12:30 PM To: kis-list@matronics.com ; TRICKEL MARK Subject: Re: KIS-List: Can anybody confirm this? Hello OC, How much weight do you have on your nose gear? Have you moved you main gear forward? As you may know the more weight on the nose the more energy to the shimmy. With more energy the less effective the friction damping. The geometry (pivot axis angle) could maybe use some tweaking to reduce shimmy. Mark K. -------------------------------------------- On Sun, 3/26/17, Owen Baker <bakerocb@cox.net> wrote: Subject: Re: KIS-List: Can anybody confirm this? To: kis-list@matronics.com, "TRICKEL MARK" <marktrickel@gmail.com> Date: Sunday, March 26, 2017, 11:45 AM "Owen Baker " <bakerocb@cox.net> 3/26/2017 Hello Mark, Yes. I can confirm this event. Here is the back story: 1) I was never happy with my first (#1) Lyle Hendricks round tube nose gear strut. It was very sturdy, but it had two manufacturing / design defects in my opinion. a) The bottom vertical 3/4-16 threaded stud potion was too short. This meant that a thin AN320-12 castle nut must be used instead of the normal thickness AN310-12 castle nut. This further meant that the total nut-to-stud thread interface holding the aluminum shoe and any washer stack up into place was pretty limited. I was concerned that that interface could fail and the entire shoe and nose wheel could fall off in flight. b) The cotter pin hole through the bottom of that stud did not pass through the center of the stud. This off set meant that the pin would not pass through the normal castle notches in the AN320-12 nut. A person had to grind / file the nut notches wider in order for the cotter pin to pass through the nut. This had two effects: ONE) The nut could not be rotated one notch at a time to adjust the friction keeping the shoe from shimmying on landing roll out unless each pair of notches was ground or filed wider. TWO) Grinding or filing all pairs of notches wider further reduced the nut-to-stud thread interface. 2) So my solution after over 500 flight hours with no problems other than dealing with the two irritating issues described above was to have Lyle make for me a new nose gear strut (#2) with modifications to eliminate the two issues. I also had Lyle make some other design modifications to this #2 strut assembly such as a longer threaded portion at the top of the compression rod and a welded cross bar at the bottom of the rod. The longer threaded portion at the top of the rod gave more vertical adjustment opportunity for the rod and the welded bar permitted one to hold the rod from rotating when wrenching nuts at the top of the rod. 3) The #2 strut assembly was installed and I set off on its first test flight. Unfortunately, not having any numerical figure available to measure the shimmy prevention friction for the shoe, I used the TFAR (That Feels About Right) criteria in tightening the AN310-12 nut holding the (new to me) two Belleville washers up against the aluminum shoe. TFAR worked fine for a few touch and go landings at an outlying field, but when I returned to my home field (KHEF Manassas Virginia) for one final landing trouble showed up. 4) At a very slow speed on the final landing roll out the nose wheel began to shimmy violently from side to side. This shimmy broke the two aluminum nose wheel brackets at the bottom of the fire wall and allowed the strut assembly to flop over sideways and the airplane nose to be lowered to the runway surface. The damage consisted of grinding off a small portion of the bottom of the #2 strut weldment, grinding off a bit of each wooden propeller tip, and some scrapes off the bottom of the spinner, lower engine cowl, and one of the main landing gear wheel pants. This event falls into the categories of: "No good deed goes unpunished" or "If it ain't broke, don't fix it". Take your choice. 5) The airplane was recovered to my hangar, Lyle graciously agreed to build me strut assembly #3, Prince Aircraft repaired the propeller tips, I replaced the spinner, repaired the engine cowling and the wheel pants, and had them painted. I put everything back together once I had all pieces in hand and used a 27 pound pull at the axle as my base figure for measuring the friction for tightening the AN310-12 nut. I flew again for the first time since the reported event on 10/18/2016. No nose wheel strut problems since then. Thanks again go to Lyle. Any questions? OC ==================================== From: mark_trickel Sent: Sunday, March 26, 2017 3:57 AM To: kis-list@matronics.com Subject: KIS-List: Can anybody confirm this? http://www.kathrynsreport.com/2016/08/kis-tr-1-n660c-incident-occurred-august.html OC? MT Forum - - MATRONICS WEB FORUMS - MATRONICS LIST WIKI - List Contribution Web Site - -Matt Dralle, List Admin.


    Message 12


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    Time: 04:42:02 PM PST US
    From: pastormac@comcast.net
    Subject: Re: Can anybody confirm this?
    Thank you for the info! I just got back from a 10 hour flight time with several landings. I wish we could do a fly in weekend some where for especially for us novice TR-1 owners. It would be great to just here from other experienced owners!! Steve Sent from my iPhone > On Mar 27, 2017, at 4:26 PM, Owen Baker <bakerocb@cox.net> wrote: > > 3/27/2017 > > Hello Steve, You wrote: "Is there an adjustment I can make?" > > This is very dangerous. DO NOT FLY THIS PLANE until the friction nut on the bottom of the nose gear has been properly adjusted. > See the photo from Keith Miller (thanks Keith) that is attached to this email. > > This shimmy can become violent enough to damage the nose gear linkages, collapse the nose gear, and cause the nose of the airplane to fall down and contact the runway surface. > > I recommend: > > 1) Elevate the nose of the plane so that the nose tire is off the ground. (Contact me if needed for tips on how to do this.) > > 2) Attach a fish scale to the shoe holding the nose wheel in the vicinity of the wheel axle. See how many pounds of pull that it takes to move the shoe from side to side. This is to establish what the friction level is now. If it is several pounds less than 27 pounds (which it probably is because of the shimmy) you must adjust the friction level. > > 3) Use a black sharpie pen to number the nut notch above the cotter pin head as notch 1. Make a vertical mark on the shoe above notch 1 with the sharpie. > > 4) Remove the cotter pin holding the large AN320-12 castle nut from turning. Go around the nut with the sharpie numbering each notch in sequence. This is so that you can keep track of the notch that is under the vertical mark. > > 5) Using a 1 1/8 inch box wrench tighten the nut one notch. Use an ice pick or similar item to ensure that the new nut notch and the cotter pin hole through the vertical stub are aligned. Leave the ice pick in place. > > 6) Use the fish scale again to move the shoe back and forth to ensure that you have adjusted the friction to the vicinity of 27 pounds. > > 7) Remove the ice pick and repeat 5 and 6 above if needed. When you have the desired friction level set, install a new cotter pin and lower the nose tire to the ground. > > 8) Go fly the plane. > > Any questions? > > OC > > =============================== > > From: pastormac@comcast.net > Sent: Monday, March 27, 2017 1:50 PM > To: kis-list@matronics.com > Subject: Re: KIS-List: Re: Can anybody confirm this? > > > Hi Guys, > Speaking of the nose gear. I'm getting quite a bit of shimmy on take off and landing. Is there an adjustment I can make? > Thanks!! > Steve > <IMG_9929.JPG>


    Message 13


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    Time: 05:13:16 PM PST US
    From: Galin Hernandez <galinhdz@gmail.com>
    Subject: Re: Can anybody confirm this?
    Sun-N-Fun is coming up. A GREAT way to meet up. I will be there Friday and Sunday. On Mon, Mar 27, 2017 at 7:36 PM, <pastormac@comcast.net> wrote: > > Thank you for the info! I just got back from a 10 hour flight time with > several landings. I wish we could do a fly in weekend some where for > especially for us novice TR-1 owners. It would be great to just here from > other experienced owners!! > Steve > > Sent from my iPhone > > > On Mar 27, 2017, at 4:26 PM, Owen Baker <bakerocb@cox.net> wrote: > > > > 3/27/2017 > > > > Hello Steve, You wrote: "Is there an adjustment I can make?" > > > > This is very dangerous. DO NOT FLY THIS PLANE until the friction nut on > the bottom of the nose gear has been properly adjusted. > > See the photo from Keith Miller (thanks Keith) that is attached to this > email. > > > > This shimmy can become violent enough to damage the nose gear linkages, > collapse the nose gear, and cause the nose of the airplane to fall down and > contact the runway surface. > > > > I recommend: > > > > 1) Elevate the nose of the plane so that the nose tire is off the > ground. (Contact me if needed for tips on how to do this.) > > > > 2) Attach a fish scale to the shoe holding the nose wheel in the > vicinity of the wheel axle. See how many pounds of pull that it takes to > move the shoe from side to side. This is to establish what the friction > level is now. If it is several pounds less than 27 pounds (which it > probably is because of the shimmy) you must adjust the friction level. > > > > 3) Use a black sharpie pen to number the nut notch above the cotter pin > head as notch 1. Make a vertical mark on the shoe above notch 1 with the > sharpie. > > > > 4) Remove the cotter pin holding the large AN320-12 castle nut from > turning. Go around the nut with the sharpie numbering each notch in > sequence. This is so that you can keep track of the notch that is under the > vertical mark. > > > > 5) Using a 1 1/8 inch box wrench tighten the nut one notch. Use an ice > pick or similar item to ensure that the new nut notch and the cotter pin > hole through the vertical stub are aligned. Leave the ice pick in place. > > > > 6) Use the fish scale again to move the shoe back and forth to ensure > that you have adjusted the friction to the vicinity of 27 pounds. > > > > 7) Remove the ice pick and repeat 5 and 6 above if needed. When you have > the desired friction level set, install a new cotter pin and lower the nose > tire to the ground. > > > > 8) Go fly the plane. > > > > Any questions? > > > > OC > > > > =============================== > > > > From: pastormac@comcast.net > > Sent: Monday, March 27, 2017 1:50 PM > > To: kis-list@matronics.com > > Subject: Re: KIS-List: Re: Can anybody confirm this? > > > > > > Hi Guys, > > Speaking of the nose gear. I'm getting quite a bit of shimmy on take off > and landing. Is there an adjustment I can make? > > Thanks!! > > Steve > > <IMG_9929.JPG> > >




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