Today's Message Index:
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     1. 01:35 PM - fun and games with a manometer (Lynn Matteson)
     2. 04:02 PM - Re: fun and games with a manometer (Lloyd & Lorrie Cudnohufsky)
     3. 05:52 PM - Re: fun and games with a manometer (Lowell Fitt)
     4. 06:16 PM - Re: fun and games with a manometer (Lynn Matteson)
     5. 06:51 PM - Re: fun and games with a manometer (Lynn Matteson)
     6. 09:34 PM - Re: fun and games with a manometer (Don Hudgeon)
 
 
 
Message 1
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| Subject:  | fun and games with a manometer | 
      
      
      I built a U-tube water manometer this week, and finally got a chance  
      to try it out (flying) today. Prior to today, I had used it to find a  
      slight leak in my pitot system, which I fixed by tightening up the  
      Nylo-Seal fittings while watching the indicated leak disappear. Ever  
      wonder how much tightening is enough for those fittings? I have, and  
      now I know....just use a manometer on the system during the assembly  
      of the fittings, and you'll know when to quit tightening.
      
      Today, I got a chance to fly briefly to test the Jabiru-dictated 2.4"  
      of water column difference between the inlet air ducts (each side  
      tested individually), and the exit-air area of the plane. I haven't  
      had any cooling problems, so I just wanted to test how close my  
      installation came to meeting that 2.4" measurement.  My installation  
      was pretty close to right on the mark...it read about 2.3" to 2.6"  
      depending on the bounce of the water in the tube. Pretty happy with  
      that, I flew home to add a 1" lip to the bottom of my cowl exit. I  
      bent a 20" length of sheet aluminum to a 60 angle, letting 1" stick  
      out into the airstream below the cowl, and c-clamped it in place. (I  
      didn't want to rivet it in place just to test the theory.)  I went up  
      and flew some more...windy day, didn't want to fly too much....and  
      now I saw about 2.5" to 3" on either of the two air ducts. But the  
      really interesting thing about the last test, was that I saw a mark  
      on the aluminum "lip" showing where it was contacting the left  
      exhaust pipe. Normally, this pipe cleared the cowl/lip by about 1/2",  
      but apparently during flight, my cowl flexes up enough to allow  
      contact with the exhaust pipe. No big deal you say, and I agree, but  
      if that lip is flexing up 1/2", what just happened to the carefully  
      engineered 3:1 ratio of exit air-to-inlet air that shouldn't change?  
      Kinda like having a wrong-way operating cowl flap for the exit air,  
      I'm thinking. So I need to stiffen up the lower cowl exit flange so  
      that it doesn't flex at all, and then do some more testing....maybe a  
      center support for the cowl is in order...something that will be  
      permanently attached to either the cowl or the airframe, but not  
      both, so as to allow for removing the cowl without having to deal  
      with another fastener down there.
      
      If anybody's having trouble with overheating issues, yet you're sure  
      of the "correctness" of your installation, you might think about the  
      rigidity of things when air pressure gets applied.
      
      Lynn Matteson
      Kitfox IV Speedster, taildragger
      Jabiru 2200, #2062
      Prince prop (64 x 30, P-tip)
      Electroair direct-fire ignition system
      Rotec TBI-40 injection (sleeved to 36mm)
      Status: flying with "Ramcharger" intake manifold...1110 hrs (since  
      3-27-2006)
      
      
Message 2
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| Subject:  | fun and games with a manometer | 
      
      
      Lynn,
      Cool stuff, (no pun intended) how did you get the tubes fastened in the cowl
      openings and did you run them into the cockpit? Look forward to hearing more
      about the experiments.
      
      Lloyd Cudnohufsky
      5 Outback 912 IVO IFA
      Northern Mi.
      
      -----Original Message-----
      From: owner-kitfox-list-server@matronics.com
      [mailto:owner-kitfox-list-server@matronics.com] On Behalf Of Lynn Matteson
      Sent: Saturday, May 28, 2011 3:34 PM
      Subject: Kitfox-List: fun and games with a manometer
      
      
      I built a U-tube water manometer this week, and finally got a chance to try
      it out (flying) today. Prior to today, I had used it to find a slight leak
      in my pitot system, which I fixed by tightening up the Nylo-Seal fittings
      while watching the indicated leak disappear. Ever wonder how much tightening
      is enough for those fittings? I have, and now I know....just use a manometer
      on the system during the assembly of the fittings, and you'll know when to
      quit tightening.
      
      Today, I got a chance to fly briefly to test the Jabiru-dictated 2.4"  
      of water column difference between the inlet air ducts (each side tested
      individually), and the exit-air area of the plane. I haven't had any cooling
      problems, so I just wanted to test how close my installation came to meeting
      that 2.4" measurement.  My installation was pretty close to right on the
      mark...it read about 2.3" to 2.6"  
      depending on the bounce of the water in the tube. Pretty happy with that, I
      flew home to add a 1" lip to the bottom of my cowl exit. I bent a 20" length
      of sheet aluminum to a 60 angle, letting 1" stick out into the airstream
      below the cowl, and c-clamped it in place. (I didn't want to rivet it in
      place just to test the theory.)  I went up and flew some more...windy day,
      didn't want to fly too much....and now I saw about 2.5" to 3" on either of
      the two air ducts. But the really interesting thing about the last test, was
      that I saw a mark on the aluminum "lip" showing where it was contacting the
      left exhaust pipe. Normally, this pipe cleared the cowl/lip by about 1/2",
      but apparently during flight, my cowl flexes up enough to allow contact with
      the exhaust pipe. No big deal you say, and I agree, but if that lip is
      flexing up 1/2", what just happened to the carefully engineered 3:1 ratio of
      exit air-to-inlet air that shouldn't change?  
      Kinda like having a wrong-way operating cowl flap for the exit air, I'm
      thinking. So I need to stiffen up the lower cowl exit flange so that it
      doesn't flex at all, and then do some more testing....maybe a center support
      for the cowl is in order...something that will be permanently attached to
      either the cowl or the airframe, but not both, so as to allow for removing
      the cowl without having to deal with another fastener down there.
      
      If anybody's having trouble with overheating issues, yet you're sure of the
      "correctness" of your installation, you might think about the rigidity of
      things when air pressure gets applied.
      
      Lynn Matteson
      Kitfox IV Speedster, taildragger
      Jabiru 2200, #2062
      Prince prop (64 x 30, P-tip)
      Electroair direct-fire ignition system
      Rotec TBI-40 injection (sleeved to 36mm)
      Status: flying with "Ramcharger" intake manifold...1110 hrs (since
      3-27-2006)
      
      
Message 3
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| Subject:  | Re: fun and games with a manometer | 
      
      
      Sorry Lynn.  Don't buy your experimentation.  These forums are reserved for 
      opinions only.
      
      Seriously, I am helping a friend finish a Series V and was interested in the 
      3:1 ratio.  I did a rough measurement on the in vs. out and interestingly 
      enough, the out only comes close to equaling the inlet area, but not quite. 
      I am curious if cooling is an issue with these since the radiator and oil 
      cooler are inside the cowl.
      
      Lowell
      --------------------------------------------------
      From: "Lynn Matteson" <lynnmatt@jps.net>
      Sent: Saturday, May 28, 2011 1:33 PM
      Subject: Kitfox-List: fun and games with a manometer
      
      >
      > I built a U-tube water manometer this week, and finally got a chance  to 
      > try it out (flying) today. Prior to today, I had used it to find a  slight 
      > leak in my pitot system, which I fixed by tightening up the  Nylo-Seal 
      > fittings while watching the indicated leak disappear. Ever  wonder how 
      > much tightening is enough for those fittings? I have, and  now I 
      > know....just use a manometer on the system during the assembly  of the 
      > fittings, and you'll know when to quit tightening.
      >
      > Today, I got a chance to fly briefly to test the Jabiru-dictated 2.4"  of 
      > water column difference between the inlet air ducts (each side  tested 
      > individually), and the exit-air area of the plane. I haven't  had any 
      > cooling problems, so I just wanted to test how close my  installation came 
      > to meeting that 2.4" measurement.  My installation  was pretty close to 
      > right on the mark...it read about 2.3" to 2.6"  depending on the bounce of 
      > the water in the tube. Pretty happy with  that, I flew home to add a 1" 
      > lip to the bottom of my cowl exit. I  bent a 20" length of sheet aluminum 
      > to a 60 angle, letting 1" stick  out into the airstream below the cowl, 
      > and c-clamped it in place. (I  didn't want to rivet it in place just to 
      > test the theory.)  I went up  and flew some more...windy day, didn't want 
      > to fly too much....and  now I saw about 2.5" to 3" on either of the two 
      > air ducts. But the  really interesting thing about the last test, was that 
      > I saw a mark  on the aluminum "lip" showing where it was contacting the 
      > left  exhaust pipe. Normally, this pipe cleared the cowl/lip by about 
      > 1/2",  but apparently during flight, my cowl flexes up enough to allow 
      > contact with the exhaust pipe. No big deal you say, and I agree, but  if 
      > that lip is flexing up 1/2", what just happened to the carefully 
      > engineered 3:1 ratio of exit air-to-inlet air that shouldn't change? 
      > Kinda like having a wrong-way operating cowl flap for the exit air,  I'm 
      > thinking. So I need to stiffen up the lower cowl exit flange so  that it 
      > doesn't flex at all, and then do some more testing....maybe a  center 
      > support for the cowl is in order...something that will be  permanently 
      > attached to either the cowl or the airframe, but not  both, so as to allow 
      > for removing the cowl without having to deal  with another fastener down 
      > there.
      >
      > If anybody's having trouble with overheating issues, yet you're sure  of 
      > the "correctness" of your installation, you might think about the 
      > rigidity of things when air pressure gets applied.
      >
      > Lynn Matteson
      > Kitfox IV Speedster, taildragger
      > Jabiru 2200, #2062
      > Prince prop (64 x 30, P-tip)
      > Electroair direct-fire ignition system
      > Rotec TBI-40 injection (sleeved to 36mm)
      > Status: flying with "Ramcharger" intake manifold...1110 hrs (since 
      > 3-27-2006)
      >
      >
      > 
      
      
Message 4
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| Subject:  | Re: fun and games with a manometer | 
      
      
      When you said "radiator" I assumed Rotax, right? I'm not sure if the  
      3:1 ratio still holds for a water-cooled engine...I have always held  
      to the 3:1 ratio for air-cooled, starting back in my radio-control  
      days, and when I got to the Jabiru camp (6 years ago), the first  
      thing I heard there was 3:1...or 4:1, or 5:1 even!  I'm not sure  
      Jabiru knew back then, just what was required.  They seem to do ok in  
      their own planes, but area little sketchy when it comes to advice for  
      homebuilts.
      Probably better off looking to Rotax for an answer to that one,  
      Lowell, if that IS what it's powered with.
      
      Lynn Matteson
      Kitfox IV Speedster, taildragger
      Jabiru 2200, #2062
      Prince prop (64 x 30, P-tip)
      Electroair direct-fire ignition system
      Rotec TBI-40 injection (sleeved to 36mm)
      Status: flying with "Ramcharger" intake manifold...1110 hrs (since  
      3-27-2006)
      
      
      On May 28, 2011, at 8:50 PM, Lowell Fitt wrote:
      
      > <lcfitt@sbcglobal.net>
      >
      > Sorry Lynn.  Don't buy your experimentation.  These forums are  
      > reserved for opinions only.
      >
      > Seriously, I am helping a friend finish a Series V and was  
      > interested in the 3:1 ratio.  I did a rough measurement on the in  
      > vs. out and interestingly enough, the out only comes close to  
      > equaling the inlet area, but not quite. I am curious if cooling is  
      > an issue with these since the radiator and oil cooler are inside  
      > the cowl.
      >
      > Lowell
      
      
Message 5
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| Subject:  | Re: fun and games with a manometer | 
      
      
      Hi Lloyd-
      
      The Jabiru engine has a pair of cooling ducts made of fiberglas, and  
      they suggest attaching the tubes (I used 1/4" OD aluminum tubing)  
      right to the ducts. I drilled into the duct, right between the spark  
      plugs, and JB Welded them in place, but any location thereabouts  
      should give you the same pressure, within reason. From these short  
      tubes, I connected to 1/4" rigid poly-something tubing (hardware  
      store stuff) with surgical tubing. The surgical tubing was a slightly  
      loose fit on the poly tubing, but would not pull off. I figured this  
      might leak a little bit so I rolled back the end of the surgical  
      tubing back over itself, and that made an almost impossible-to-remove  
      connection. Anyway, getting back to the run of the tubing, I ran the  
      poly tubing through an available hole...don't we all have one of  
      those in our firewall someplace?...and up and over my glare shield. I  
      stopped them there and made the connection to the manometer, again  
      with surgical tubing.
      
      Oh, yeah, the manometer I built was similar to the one in:       
      http://www.iflyez.com/manometer.shtml       but I made mine with an  
      aluminum plate instead of wood (gave me another chance to play with  
      the TIG), and used smaller tubing than the 3/8" suggested in that  
      article.
      
      At first I used tap water and detergent and food coloring, and like  
      they say in the article, "you'll wait HOURS for the bubbles to  
      settle", so then I used distilled water, a dab of softener to break  
      the surface tension, and food coloring, and this time the water just  
      slides up and down the walls of the tubing without hesitation. These  
      things are so simple to make, but the trick is to print the scale to  
      *exactly* the dimension given...for accuracy. I converted the knots  
      numbers to "miles per hour" and checked my airspeed indicator after  
      first checking for leaks. I found that my airspeed was 2 miles under  
      at 60 mph, right on at 100 mph, and 1 mile over at 140 mph....close  
      enough for a Kitfox, in my book. : )
      
      Lynn Matteson
      Kitfox IV Speedster, taildragger
      Jabiru 2200, #2062
      Prince prop (64 x 30, P-tip)
      Electroair direct-fire ignition system
      Rotec TBI-40 injection (sleeved to 36mm)
      Status: flying with "Ramcharger" intake manifold...1110 hrs (since  
      3-27-2006)
      
      
      On May 28, 2011, at 6:59 PM, Lloyd & Lorrie Cudnohufsky wrote:
      
      > <7suds@chartermi.net>
      >
      > Lynn,
      > Cool stuff, (no pun intended) how did you get the tubes fastened in  
      > the cowl
      > openings and did you run them into the cockpit? Look forward to  
      > hearing more
      > about the experiments.
      >
      > Lloyd Cudnohufsky
      > 5 Outback 912 IVO IFA
      > Northern Mi.
      
      
Message 6
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  | 
      
      
| Subject:  | Re: fun and games with a manometer | 
      
      More Manometer Stuff
      
      Hi Guys
      
      I use a manometer to balance the carbs on my 912. I connect each end of the
      U-Shaped clear tubing to each nipple on the intake manifolds where the
      balance tube goes. I loop the tubing around a yard stick and put a small
      amount of Rislone in the tube. All that is necessary to do is adjust the
      throttle linkage so that the Rislone level is EXACTLY the same on each side
      of the loop. This instrument is very accurate and very  small adjustments
      are all that is necessary.
      Just to be sure I have recently bought a "Carbmate electronic balancer" as a
      check on my adjustments but the manometer is every bit as accurate!! Cost
      about $2 compared to $110.
      
      Have fun
      
      Don Hudgeon
      Vixen 912UL   IVO IFA
      
      
      On Sat, May 28, 2011 at 6:48 PM, Lynn Matteson <lynnmatt@jps.net> wrote:
      
      >
      > Hi Lloyd-
      >
      > The Jabiru engine has a pair of cooling ducts made of fiberglas, and they
      > suggest attaching the tubes (I used 1/4" OD aluminum tubing) right to the
      > ducts. I drilled into the duct, right between the spark plugs, and JB Welded
      > them in place, but any location thereabouts should give you the same
      > pressure, within reason. From these short tubes, I connected to 1/4" rigid
      > poly-something tubing (hardware store stuff) with surgical tubing. The
      > surgical tubing was a slightly loose fit on the poly tubing, but would not
      > pull off. I figured this might leak a little bit so I rolled back the end of
      > the surgical tubing back over itself, and that made an almost
      > impossible-to-remove connection. Anyway, getting back to the run of the
      > tubing, I ran the poly tubing through an available hole...don't we all have
      > one of those in our firewall someplace?...and up and over my glare shield. I
      > stopped them there and made the connection to the manometer, again with
      > surgical tubing.
      >
      > Oh, yeah, the manometer I built was similar to the one in:
      > http://www.iflyez.com/manometer.shtml       but I made mine with an
      > aluminum plate instead of wood (gave me another chance to play with the
      > TIG), and used smaller tubing than the 3/8" suggested in that article.
      >
      > At first I used tap water and detergent and food coloring, and like they
      > say in the article, "you'll wait HOURS for the bubbles to settle", so then I
      > used distilled water, a dab of softener to break the surface tension, and
      > food coloring, and this time the water just slides up and down the walls of
      > the tubing without hesitation. These things are so simple to make, but the
      > trick is to print the scale to *exactly* the dimension given...for accuracy.
      > I converted the knots numbers to "miles per hour" and checked my airspeed
      > indicator after first checking for leaks. I found that my airspeed was 2
      > miles under at 60 mph, right on at 100 mph, and 1 mile over at 140
      > mph....close enough for a Kitfox, in my book. : )
      >
      >
      > Lynn Matteson
      > Kitfox IV Speedster, taildragger
      > Jabiru 2200, #2062
      > Prince prop (64 x 30, P-tip)
      > Electroair direct-fire ignition system
      > Rotec TBI-40 injection (sleeved to 36mm)
      > Status: flying with "Ramcharger" intake manifold...1110 hrs (since
      > 3-27-2006)
      >
      >
      > On May 28, 2011, at 6:59 PM, Lloyd & Lorrie Cudnohufsky wrote:
      >
      >> 7suds@chartermi.net>
      >>
      >> Lynn,
      >> Cool stuff, (no pun intended) how did you get the tubes fastened in the
      >> cowl
      >> openings and did you run them into the cockpit? Look forward to hearing
      >> more
      >> about the experiments.
      >>
      >> Lloyd Cudnohufsky
      >> 5 Outback 912 IVO IFA
      >> Northern Mi.
      >>
      >
      >
      
 
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