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     1. 12:53 PM - Flight Test Update - N776PM (Paul Mulwitz)
     2. 07:17 PM - Re: Flight Test Update - N776PM (Michel Therrien)
 
 
 
Message 1
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| Subject:  | Flight Test Update - N776PM | 
      
      
      It's been a little over two months since my Zodiac XL got its 
      airworthiness certificate.  Yesterday I had my first flight with no 
      squawks.  I figured it is time to spread the word on the things I 
      found.  Current flight time is around 17 hours.  My typical test flight 
      was just over one half hour with just one landing.  This might have been 
      a bit shorter if I didn't have to get out from under a class C terminal 
      area before climbing to a reasonable test altitude.
      
      Yesterday the air was reasonably cool - around 60 on the ground so it 
      must have been around 45 at 5000 MSL where I did my testing.  At full 
      throttle the engine ran smoothly and the plane indicated around 120 
      knots.  I have not calibrated the airspeed yet, but casual comparison 
      with GPS ground speed suggests it is pretty close to correct.  I have a 
      Jabiru 3300A with wood Sensenich 64ZK49 propeller (standard stuff when 
      you buy the FWF package from Pete at USA Jabiru).  Cylinder head 
      temperatures were all green with the highest around 320.  Oil 
      temperature was around 170.  At WOT engine RPM was just over 3000 RPM at 
      5000 MSL.  CHTs in full throttle climb were around 1100 and in high 
      cruise around 1300.
      
      I am sure I can't remember all the problems I fixed in the first two 
      months of phase I flight test, but I'll try to recount as many as I can.
      
      1.  Engine cooling was a big problem.  My first attempt at adding rubber 
      seals at the front of the cooing ducts was not correct.  I should have 
      fitted the rubber seals carefully to the inlets in the cowl.  I also 
      needed to adjust the air dams in the right duct (cylinders 1,3,5) but 
      the other one never needed any adjustment.
      
      2.  Nose gear bearings were too tight.  The plastic bearings at both the 
      top and bottom of the nose gear column restricted movement instead of 
      just guiding it.  The nose should move up and down easily when you put 
      your weight on the propeller drive shaft.  The plastic bearings as 
      delivered from ZAC were much too tight.  I loosened them on original 
      installation but that wasn't enough.
      
      3.  Rudder does not return to center when you remove pressure from the 
      pedals.  This problem is unresolved.  It doesn't present too much of a 
      problem but it is difficult to keep the ball centered unless you give 
      the left rudder pedal a good kick after maneuvering.  A related 
      unresolved problem is the nose tends to wander in yaw - especially in 
      turbulence.  I am thinking nice thoughts of adding some sort of fixed 
      vertical stabilizer fin - probably on the bottom of the fuselage to 
      correct this.  It is not a big problem but makes flying a bit uncomfortable.
      
      4.  I had a few electronic problems with my Dynon and Garmin avionics.  
      The Dynon tachometer needed to have a resistor installed in line with 
      the connection to the alternator (through a fuse).  Before adding the 
      resistor the tachometer went nuts in mid range power settings but worked 
      fine above 2200 RPM and below 1700.
      
      The only problem with the Garmin stuff was I needed to attach a pin to 
      ground to enable the built-in intercom on my SL-30.  I also had issues 
      setting the squelch, but that was just an operator issue.
      
      5.  Several times I had the quick drains in the fuel tanks turn into 
      slow leaks.  This was caused by tiny pieces of aluminum getting caught 
      in the tiny O-ring that seals the quick drain.  I got an extra quick 
      drain valve and learned how to replace a faulty one with a pail under 
      the stream of fuel to collect that fuel that escapes between the time I 
      remove one and install the other one.  Then it is a relatively simple 
      task to clean out the defective seal and put it aside for the next 
      occurrence of this problem.
      
      6.  At one point I discovered the carburetor was barely attached to the 
      engine.  It was held in place by the air intake hose but this was still 
      a bit scary.  It was easy to loosen both hose clamps that hold the 
      carburetor and push it firmly in place before tightening the clamps again.
      
      7.  Another carburetor problem -- the small hose connecting the 
      carburetor to the air box came off.  This caused the engine to drop out 
      randomly with RPM dropping about 500 revs in turbulence when I reduced 
      power for descent.  The engine ran more smoothly when I added power to 
      cruise levels.  The original hose had a 3/16 ID and was quite loose on 
      the carburetor nipple.  I got some vinyl hose with .170 ID at the 
      hardware store and it holds on and works just fine.
      
      8.  Elevator trim was not powerful enough to trim pitch when any flaps 
      were employed.  I added an extra fixed tab to the rear of the original 
      one and found improvement but I was still unable to get neutral trim 
      with full flaps.  A bigger tab fixed this.  I think the final extra tab 
      was around 20 square inches to neutralize 20 degrees of flaps.
      
      9.  I had a lot of trouble getting the rudder into a neutral position in 
      flight.  The nose gear centers when there is no weight on the gear and 
      the connections through the pedals and rudder cables pulls the rudder 
      one way or the other until you get this properly adjusted.  This took me 
      many small changes.  At one point I didn't like the number of exposed 
      threads in one of the turnbuckles and learned you can get forks that are 
      about a  half inch longer than the normal ones to give you more 
      adjustment room.  I only needed one of these extra length forks to allow 
      more "Left" rudder in the cable setup.  (I am getting really good at 
      installing safety wire in turnbuckles.)
      
      In all my experience at being a test pilot for an amateur (me) built 
      aircraft has been quite an experience.  The only time I felt at all 
      scared was when the engine was cutting out.  Mostly it has been a matter 
      of getting all the little adjustments made to make the plane fly 
      properly.  Now, I am looking forward to spending some time in the 
      pattern learning how to do really nice approaches and landings.
      
      Paul
      Camas, WA
      
      
Message 2
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| Subject:  | Re: Flight Test Update - N776PM | 
      
      
      Thanks for sharing Paul.  Now you should start to really enjoy your toy.   
      
      Do not archive
      
      Sent from my iPad
      
      On Sep 20, 2011, at 15:50, Paul Mulwitz <psm@att.net> wrote:
      
      > 
      > It's been a little over two months since my Zodiac XL got its airworthiness certificate.
      Yesterday I had my first flight with no squawks.  I figured it is
      time to spread the word on the things I found.  Current flight time is around
      17 hours.  My typical test flight was just over one half hour with just one landing.
      This might have been a bit shorter if I didn't have to get out from under
      a class C terminal area before climbing to a reasonable test altitude.
      > 
      > Yesterday the air was reasonably cool - around 60 on the ground so it must have
      been around 45 at 5000 MSL where I did my testing.  At full throttle the engine
      ran smoothly and the plane indicated around 120 knots.  I have not calibrated
      the airspeed yet, but casual comparison with GPS ground speed suggests it
      is pretty close to correct.  I have a Jabiru 3300A with wood Sensenich 64ZK49
      propeller (standard stuff when you buy the FWF package from Pete at USA Jabiru).
      Cylinder head temperatures were all green with the highest around 320.  Oil
      temperature was around 170.  At WOT engine RPM was just over 3000 RPM at 5000
      MSL.  CHTs in full throttle climb were around 1100 and in high cruise around
      1300.
      > 
      > I am sure I can't remember all the problems I fixed in the first two months of
      phase I flight test, but I'll try to recount as many as I can.
      > 
      > 1.  Engine cooling was a big problem.  My first attempt at adding rubber seals
      at the front of the cooing ducts was not correct.  I should have fitted the
      rubber seals carefully to the inlets in the cowl.  I also needed to adjust the
      air dams in the right duct (cylinders 1,3,5) but the other one never needed any
      adjustment.
      > 
      > 2.  Nose gear bearings were too tight.  The plastic bearings at both the top
      and bottom of the nose gear column restricted movement instead of just guiding
      it.  The nose should move up and down easily when you put your weight on the
      propeller drive shaft.  The plastic bearings as delivered from ZAC were much too
      tight.  I loosened them on original installation but that wasn't enough.
      > 
      > 3.  Rudder does not return to center when you remove pressure from the pedals.
      This problem is unresolved.  It doesn't present too much of a problem but it
      is difficult to keep the ball centered unless you give the left rudder pedal
      a good kick after maneuvering.  A related unresolved problem is the nose tends
      to wander in yaw - especially in turbulence.  I am thinking nice thoughts of
      adding some sort of fixed vertical stabilizer fin - probably on the bottom of
      the fuselage to correct this.  It is not a big problem but makes flying a bit
      uncomfortable.
      > 
      > 4.  I had a few electronic problems with my Dynon and Garmin avionics.  The Dynon
      tachometer needed to have a resistor installed in line with the connection
      to the alternator (through a fuse).  Before adding the resistor the tachometer
      went nuts in mid range power settings but worked fine above 2200 RPM and below
      1700.
      > 
      > The only problem with the Garmin stuff was I needed to attach a pin to ground
      to enable the built-in intercom on my SL-30.  I also had issues setting the squelch,
      but that was just an operator issue.
      > 
      > 5.  Several times I had the quick drains in the fuel tanks turn into slow leaks.
      This was caused by tiny pieces of aluminum getting caught in the tiny O-ring
      that seals the quick drain.  I got an extra quick drain valve and learned
      how to replace a faulty one with a pail under the stream of fuel to collect that
      fuel that escapes between the time I remove one and install the other one.
      Then it is a relatively simple task to clean out the defective seal and put it
      aside for the next occurrence of this problem.
      > 
      > 6.  At one point I discovered the carburetor was barely attached to the engine.
      It was held in place by the air intake hose but this was still a bit scary.
      It was easy to loosen both hose clamps that hold the carburetor and push it
      firmly in place before tightening the clamps again.
      > 
      > 7.  Another carburetor problem -- the small hose connecting the carburetor to
      the air box came off.  This caused the engine to drop out randomly with RPM dropping
      about 500 revs in turbulence when I reduced power for descent.  The engine
      ran more smoothly when I added power to cruise levels.  The original hose
      had a 3/16 ID and was quite loose on the carburetor nipple.  I got some vinyl
      hose with .170 ID at the hardware store and it holds on and works just fine.
      > 
      > 8.  Elevator trim was not powerful enough to trim pitch when any flaps were employed.
      I added an extra fixed tab to the rear of the original one and found
      improvement but I was still unable to get neutral trim with full flaps.  A bigger
      tab fixed this.  I think the final extra tab was around 20 square inches
      to neutralize 20 degrees of flaps.
      > 
      > 9.  I had a lot of trouble getting the rudder into a neutral position in flight.
      The nose gear centers when there is no weight on the gear and the connections
      through the pedals and rudder cables pulls the rudder one way or the other
      until you get this properly adjusted.  This took me many small changes.  At
      one point I didn't like the number of exposed threads in one of the turnbuckles
      and learned you can get forks that are about a  half inch longer than the normal
      ones to give you more adjustment room.  I only needed one of these extra
      length forks to allow more "Left" rudder in the cable setup.  (I am getting really
      good at installing safety wire in turnbuckles.)
      > 
      > In all my experience at being a test pilot for an amateur (me) built aircraft
      has been quite an experience.  The only time I felt at all scared was when the
      engine was cutting out.  Mostly it has been a matter of getting all the little
      adjustments made to make the plane fly properly.  Now, I am looking forward
      to spending some time in the pattern learning how to do really nice approaches
      and landings.
      > 
      > Paul
      > Camas, WA
      > 
      > 
      > 
      > 
      
      
 
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